Case studyread the incident scenario and write a response


Case StudyRead the incident scenario, and write a response that is at least three pages in length. Your response must includeanswers to the questions being asked. All sources used, including the textbook, must be referenced. Paraphrased and/orquoted materials must have accompanying in-text and reference citations in APA format.Scenario:You are the Refinery Emergency Response Coordinator for an incident at the SJV Refinery which has been in operationsince 1966. The refinery processes 120,000 bbls of crude oil per day, which has a sulfur content of 2.5 percent. Therefinery converts crude oil to naptha, light oil, and heavy oils using the Atmospheric/Vacuum Distillation Unit with keyequipment such as the following:? naptha, kerosene, gasoline, and diesel hydrotreaters;? isomerization unit;? naptha reformer;? fluid catalytic cracker;? coker;? hydrocracker;? polymerization unit (petrochemical section of the refinery polymerizing olefin gases to produce polyethylene);? sulfur recovery Claus plant (catalytic reactors); and? distillate/gasoline blending tanks.The refinery was initiating work on a major plant turnaround at the time of the incident to complete required maintenancerepairs, mechanical integrity inspections, and modifications to existing equipment. Twenty contractor companies(approximately 150 employees) have been contracted to perform this work under the direction of refinery staff. All of thecontractor workers completed the refinery orientation training.Work for the contractor crews is assigned/scheduled each morning. On the day of the incident, the day-shift (6 am to 6pm) crew had been tasked with isolating the acid gas feed stream for the Claus unit. Due to other work priorities, the crewdid not isolate the line as planned. A shift turnover for the night contractor crew did not happen due to mandatory safetytraining that delayed their arrival at the worksite. Upon their arrival at the work site, the night crew held a job safetyanalysis (JSA) review of the scheduled task (line breaking of the acid gas feed line to replace a segment) to be performedand the hazards present. No pressure gauges or monitoring was present to indicate that the acid gas feed line wasoperational. The crew initiated the line breaking activity (open the line to the atmosphere) at approximately 7:45 pm underself-contained breathing apparatus (SCBA), which almost immediately resulted in the uncontrolled release of acid gas. Anearby ignition source from a welding operation ignited the flammable gas. The following actions were initially taken:? The evacuation alarm was sounded and the refinery emergency response team (ERT) was activated.? The plant manager and the local fire department were notified of the incident.? The incident command was established at the refinery office near the main refinery access gate to the south (thisis the furthest distance within the refinery boundary from the incident location).? The refinery ERT incident commander implemented actions required under the approved refinery emergencyresponse plan.? The ERT was not able to immediately isolate the acid gas feed pipeline.? The fire department arrived on location and assumed the incident command of the event.Additional Relevant Information:? The refinery encompasses an area measuring 2000 feet by 1400 feet. The Claus unit is located in the mostnorthern part of the refinery, approximately 1350 feet from the main refinery access gate to the south. Thepolymerization unit is operating directly adjacent to the Claus unit. BOS 3640, Interactions of Hazardous Materials 4? The nearest residential community is located approximately 1000 feet to the northeast of the refinery.? A plastic recycling plant is located along the south fence boundary of the refinery.? A major interstate highway runs directly parallel to the plant, approximately 1/4 of a mile directly north of therefinery.? The ambient temperature on the day of the incident was 85° F and the wind was blowing at 7 mph from thesouthwest to the northeast.? Work crews were scheduled to work 12-hour shifts, 24-hours a day, to complete the refinery turnaround.? Due to the age of the refinery, SJV has implemented a robust mechanical integrity program.? The refinery has a trained ERT that can respond to incidents.? Fixed water monitors are present throughout the refinery to extinguish refinery equipment fires. The refinery ERTdoes not fight fires past the incipient stage.? The refinery has received notices of violation (NOVs) from the local air district in the past several years due to gasand liquid leaks from piping components, such as valves, compressor/pump seals, and for excess sodium dioxide(SO2) emissions related with their sulfur plant.? Due to historical discharges of organic compounds, groundwater monitoring wells are present down gradient ofthe facility. Groundwater underlying the plant has historically been encountered at 30 feet below ground surface.? Hydrogen sulfide is present in the acid gas feed to the Claus plant. The H2S concentration of the acid gas feed isapproximately 70 percent by volume. H2S and sulfur dioxide (SO2) have the following physical properties:.

Discuss the hazards posed by the interaction of the hazardous materials present at the refinery and adjacentfacilities, including the resulting by-products of the incident fire and acid gas release.2. As the lead refinery representative on the unified incident command (UIC), what actions should be taken by theUIC to respond to this incident (please consider all receptors).3. If the polymerization unit is engulfed in the fire, how will this affect your response?4. All emergency responders participated in the post-incident critique. What corrective actions should beimplemented by the refinery to prevent the reoccurrence of this incident?

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Chemistry: Case studyread the incident scenario and write a response
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